AlphAndruino Posté(e) Avril 21, 2024 Posté(e) Avril 21, 2024 (modifié) Salut, Ca y est, j'ai passé le cap, j'ai fait mon installation hier. Pas de problèmes particuliers hormis avec le bl-touch. Lors du home du Z, la tête se positionne au milieu de l'axe X et fait son home, alors qu'elle devrait positionner le bl-ltouch au centre du plateau conformément à l'offset, j'ai essayé plusieurs valeurs d'offset de la sonde mais rien ne change, j'aurais loupé un truc? Et bien sûr, impossible de faire un bed levelling, j'ai une erreur Move out of range quand la tête arrive à droite Voici mon fichier printer.cfg : [include mainsail.cfg] [stepper_x] step_pin: ar54 dir_pin: ar55 enable_pin: !ar38 microsteps: 16 rotation_distance: 40 endstop_pin: ^!ar3 position_endstop: 0 position_max: 310 homing_speed: 60.0 [stepper_y] step_pin: ar60 dir_pin: ar61 enable_pin: !ar56 microsteps: 16 rotation_distance: 40 endstop_pin: ^!ar14 position_endstop: 0 position_max: 310 homing_speed: 60 homing_positive_dir: false [stepper_z] step_pin: ar46 dir_pin: !ar48 enable_pin: !ar62 microsteps: 16 rotation_distance: 8 endstop_pin: probe:z_virtual_endstop position_min: -3 position_max: 400 homing_speed: 30 second_homing_speed: 1 [stepper_z1] step_pin: ar36 dir_pin: !ar34 enable_pin: !ar30 microsteps: 16 rotation_distance: 8 [extruder] step_pin: ar26 dir_pin: ar28 enable_pin: !ar24 microsteps: 16 rotation_distance: 7 nozzle_diameter: 0.400 filament_diameter: 1.750 heater_pin: ar10 sensor_type: EPCOS 100K B57560G104F sensor_pin: analog13 min_extrude_temp: 190 min_temp: 5 max_temp: 300 max_extrude_only_distance: 500 max_extrude_cross_section: 2.0 [heater_bed] heater_pin: ar8 sensor_type: EPCOS 100K B57560G104F sensor_pin: analog14 min_temp: 5 max_temp: 150 [fan] pin: ar9 kick_start_time: 0.500 [heater_fan my_nozzle_fan] pin:ar7 heater: extruder heater_temp: 50.0 fan_speed: 1.0 [mcu] #make sure this reflects your serial port you found when flashing klipper serial: /dev/serial/by-id/usb-1a86_USB_Serial-if00-port0 [printer] kinematics: cartesian max_velocity: 200 max_accel: 3000 max_z_velocity: 50 max_z_accel: 100 square_corner_velocity: 5 [bltouch] sensor_pin: ^ar18 control_pin: ar11 x_offset:-49 y_offset:-25 speed:10 samples:3 samples_result:average set_output_mode: 5V probe_with_touch_mode: true stow_on_each_sample: false [safe_z_home] home_xy_position: 122,183 speed: 100 z_hop: 20 z_hop_speed: 20 [bed_mesh] speed: 800 mesh_min: 30,30 mesh_max: 270,270 probe_count: 5,5 mesh_pps: 2,2 algorithm: bicubic bicubic_tension: 0.2 move_check_distance: 3.0 split_delta_z: .010 fade_start: 1.0 fade_end: 5.0 [bed_screws] screw1: 55,55 screw1_name: front left screw2: 255,55 screw2_name: front right screw3: 255,255 screw3_name: back right screw4: 55,255 screw4_name: back left speed: 100.0 [screws_tilt_adjust] screw1: 22,83 screw1_name: front left screw2: 222,83 screw2_name: front right screw3: 22,283 screw3_name: back left screw4: 222,283 screw4_name: back right speed: 100.0 screw_thread: CW-M5 #uncomment the following lines to use Z_TILT_ADJUST and uncomment G34 Macro to use G34 #[z_tilt] #z_positions: # 10,155 # 270,155 # #points: # 10,155 # 270,155 #speed: 100 #horizontal_move_z: 10 [gcode_macro G29] gcode: BED_MESH_CLEAR G28 BED_MESH_CALIBRATE BED_MESH_PROFILE SAVE=x1 #[gcode_macro G34] #gcode: # G28 # Z_TILT_ADJUST [gcode_macro G35] gcode: G28 SCREWS_TILT_CALCULATE [gcode_macro START_PRINT] # Reference https://github.com/KevinOConnor/klipper/blob/master/docs/Config_Reference.md#gcode_macroA # On how to override default parameters #default_parameter_BED_TEMP: 60 #default_parameter_EXTRUDER_TEMP: 200 gcode: # Home the printer G28 #Probe Everytime G29 #load saved mesh at print start instead of probe. Uncomment to use but comment out G29 #BED_MESH_PROFILE LOAD=x1 # Use absolute coordinates G90 # Move the nozzle near the bed G1 X0 Y0 Z5 F3000 # Move the nozzle very close to the bed G1 Z0.15 F300 G92 E0 ;Reset Extruder G1 X20 Y5 Z0.3 F5000.0 G1 Z0.3 F1000 G1 X200 Y5 F1500.0 E15 G1 X200 Y5.3 Z0.3 F5000.0 G1 X5.3 Y5.3 Z0.3 F1500.0 E30 G1 Z3 F3000 G21 ; set units to millimeters G90 ; use absolute coordinates M83 ; use relative distances for extrusion G92 E0 [gcode_macro END_PRINT] gcode: # Turn off bed, extruder, and fan M140 S0 M104 S0 M106 S0 # Move nozzle away from print while retracting G91 G1 X-2 Y-2 E-3 F300 # Raise nozzle by 10mm G1 Z30 F3000 G90 # Disable steppers M84 [pause_resume] recover_velocity: 50. #[filament_switch_sensor my_sensor] #Move filament runout sensor from TFT to X+ endstop pin. Uncomment all but this line if you want to use this #pause_on_runout: False #runout_gcode: PAUSE #insert_gcode: RESUME #switch_pin: ar2 # Arduino aliases for atmega2560/1280 (Arduino mega) boards [board_pins arduino-mega] aliases: ar0=PE0, ar1=PE1, ar2=PE4, ar3=PE5, ar4=PG5, ar5=PE3, ar6=PH3, ar7=PH4, ar8=PH5, ar9=PH6, ar10=PB4, ar11=PB5, ar12=PB6, ar13=PB7, ar14=PJ1, ar15=PJ0, ar16=PH1, ar17=PH0, ar18=PD3, ar19=PD2, ar20=PD1, ar21=PD0, ar22=PA0, ar23=PA1, ar24=PA2, ar25=PA3, ar26=PA4, ar27=PA5, ar28=PA6, ar29=PA7, ar30=PC7, ar31=PC6, ar32=PC5, ar33=PC4, ar34=PC3, ar35=PC2, ar36=PC1, ar37=PC0, ar38=PD7, ar39=PG2, ar40=PG1, ar41=PG0, ar42=PL7, ar43=PL6, ar44=PL5, ar45=PL4, ar46=PL3, ar47=PL2, ar48=PL1, ar49=PL0, ar50=PB3, ar51=PB2, ar52=PB1, ar53=PB0, ar54=PF0, ar55=PF1, ar56=PF2, ar57=PF3, ar58=PF4, ar59=PF5, ar60=PF6, ar61=PF7, ar62=PK0, ar63=PK1, ar64=PK2, ar65=PK3, ar66=PK4, ar67=PK5, ar68=PK6, ar69=PK7, analog0=PF0, analog1=PF1, analog2=PF2, analog3=PF3, analog4=PF4, analog5=PF5, analog6=PF6, analog7=PF7, analog8=PK0, analog9=PK1, analog10=PK2, analog11=PK3, analog12=PK4, analog13=PK5, analog14=PK6, analog15=PK7, # Marlin adds these additional aliases ml70=PG4, ml71=PG3, ml72=PJ2, ml73=PJ3, ml74=PJ7, ml75=PJ4, ml76=PJ5, ml77=PJ6, ml78=PE2, ml79=PE6, ml80=PE7, ml81=PD4, ml82=PD5, ml83=PD6, ml84=PH2, ml85=PH7 #*# <---------------------- SAVE_CONFIG ----------------------> #*# DO NOT EDIT THIS BLOCK OR BELOW. The contents are auto-generated. #*# #*# [extruder] #*# control = pid #*# pid_kp = 21.465 #*# pid_ki = 0.980 #*# pid_kd = 117.521 #*# #*# [heater_bed] #*# control = pid #*# pid_kp = 48.362 #*# pid_ki = 0.638 #*# pid_kd = 915.854 #*# #*# [bltouch] #*# z_offset = 2.045 #*# #*# [bed_mesh default] #*# version = 1 #*# points = #*# 0.000000, 0.032500, 0.040000, 0.105000, 0.195000 #*# -0.037500, -0.045000, -0.005000, 0.045000, 0.112500 #*# -0.002500, -0.015000, 0.005000, 0.062500, 0.145000 #*# 0.115000, 0.077500, 0.055000, 0.080000, 0.080000 #*# 0.072500, 0.035000, 0.020000, 0.015000, 0.055000 #*# x_count = 5 #*# y_count = 5 #*# mesh_x_pps = 2 #*# mesh_y_pps = 2 #*# algo = bicubic #*# tension = 0.2 #*# min_x = 30.0 #*# max_x = 270.0 #*# min_y = 30.0000000001 #*# max_y = 270.0 #*# #*# [bed_mesh x1] #*# version = 1 #*# points = #*# 0.000000, 0.032500, 0.040000, 0.105000, 0.195000 #*# -0.037500, -0.045000, -0.005000, 0.045000, 0.112500 #*# -0.002500, -0.015000, 0.005000, 0.062500, 0.145000 #*# 0.115000, 0.077500, 0.055000, 0.080000, 0.080000 #*# 0.072500, 0.035000, 0.020000, 0.015000, 0.055000 #*# x_count = 5 #*# y_count = 5 #*# mesh_x_pps = 2 #*# mesh_y_pps = 2 #*# algo = bicubic #*# tension = 0.2 #*# min_x = 30.0 #*# max_x = 270.0 #*# min_y = 30.0000000001 #*# max_y = 270.0 Voici le log d'un G29 09:08 Move out of range: 319.000 55.000 5.000 [0.000] 09:08 Move out of range: 319.000 55.000 5.000 [0.000] 09:08 probe at 259.000,55.000 is z=1.342500 09:08 probe at 259.000,55.000 is z=1.340000 09:08 probe at 259.000,55.000 is z=1.340000 09:08 probe at 199.000,55.000 is z=1.580000 09:08 probe at 199.000,55.000 is z=1.577500 09:08 probe at 199.000,55.000 is z=1.577500 09:08 probe at 139.000,55.000 is z=1.717500 09:08 probe at 139.000,55.000 is z=1.720000 09:08 probe at 139.000,55.000 is z=1.715000 09:08 probe at 79.000,55.000 is z=1.875000 09:08 probe at 79.000,55.000 is z=1.872500 09:08 probe at 79.000,55.000 is z=1.855000 09:08 G29 Modifié (le) Avril 21, 2024 par AlphAndruino
pommeverte Posté(e) Avril 21, 2024 Posté(e) Avril 21, 2024 (modifié) Salut, Comme tu as une course de 310mm en X et que tu demandes d'aller à X = 270 +49 = 319, ce n'est pas étonnant qu'elle râle ! Il suffit donc de modifier la surface de palpage: mesh_max: 260,270 PS: question de néophyte en X1 : il y a 17 minutes, AlphAndruino a dit : screw_thread: CW-M5 les vis de réglage sont si grosses (M5) ? Modifié (le) Avril 21, 2024 par pommeverte
AlphAndruino Posté(e) Avril 21, 2024 Auteur Posté(e) Avril 21, 2024 (modifié) OK, j'avais joué sur ce paramètre mais je ne l'avais pas compris il y a une heure, pommeverte a dit : les vis de réglage sont si grosses (M5) Oui, 5mm de diamètre Modifié (le) Avril 21, 2024 par AlphAndruino 1
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